D8110 [20110]
|
In service. working some Permanent Way trains as well
as shunt releases at weekends for Santa specials. But the old compressor
oil is once again due an oil change. Two weeks before Christmas the loco
was derailed on the points just outside the box towards the bridge. Damage
to sand pipe and life guard were swiftly repaired. |
[D8118] 20118
|
By the second weekend of October the two body side door
panels, removed earlier due to paint faults, were back on the loco. Some
more doors have been found with the paint bubbling up in places. These
have now had the same treatment as the first two, and were all back on
by the end of November. A start has been made to find the leak in the turbo
which is in the workshop. It has been part dismantled, but due to the need
for special tools etc, it has been put back together for the time being.
It has also been found that the two spare turbochargers are both the same,
both right hand. So this will mean that the left hand turbocharger will
have to go away for repair at some stage, to a specialist firm in Birkenhead,
Liverpool. With the turbochargers out some cleaning and repainting has
taken place. We will use the turbochargers from the spare engine in store.
They should be at Buckfastleigh by early 2002 were they will be cleaned,
repainted and have the oil in them changed prior to refitting on to the
loco. |
D7612 [25262, 25901]
|
Work has started on body side repairs with the patchy
filler being knocked out and damaged metal cut away from the cab area only
to reveal a well rusted floor. The roof panel around the exhaust stack
was removed to reveal a rusted out exhaust stack. This is now on the floor
in the workshop. A new one will have to be made.
Tuesday 30th October saw the loco put outside after all
the welding was finished and a coat of primer and undercoat applied to
the treated parts. A full repaint will now take place during 2002 after
the cooler group has been lifted out and repaired. Whilst inside the workshop
the batteries were checked over, and all needed topping up. The duff one
was found, and it was an old block of four, one cell read 1.5 volts whilst
the next one read 3.5volts. All the rest read between 2.2 - 2.4 volts,
with this sort of reading from the batteries a new set may not be needed
just yet; lets hope! By the end of November the No.2 cab was all back together
with the bare bits of paint work repainted, the AWS valve that was leaking
air onto the bulkhead above the drivers head was also repaired. Work
on the No.1 end cab has at long last been started, with most of the paint
work be attended to.
Below is a T.O.P.S. printout for the loco, with only
six months left in service. It was working with 25908 on a sand train from
Over & Wharton (Nr Winsford just north of Crewe) to Reading West Junction
with a load of 25 wagons totalling 888 tons and it departed 2 hours &
20 minutes late at 15.20; the headcode was 7Z38.
|
Class 09
|
Loco back outside. It was started up last on Sunday 11
th November and later that day it was drained down for the winter. |
Class 127
|
Back as a three car set at the start of October. The
radiator on the Ashburton end has started to leak badly again.
A bit of history on the unit; on the morning of 7th May
1983 power car 51592 was paired with trailers 59615 & 59645 and powercar
51627. Powercar 51604 was paired with trailers 59637 & 59617and
powercar 51606. Both sets were in St. Pancras between 07.15 &
07.45.
The set, as preserved, ran an owners special in December
and has now been drain down for the winter. |
Class 122 - 55000
|
By the end of the first week of October the cab windows
at the brake van end had been replaced. A few weeks later the twin exhaust
pipes were refitted to the cab front, along with a start on rebuilding
this cab. The small saloon has had it's seats refitted, and looks quite
smart. During December the batteries were washed out and refilled
with new acid. Just before Christmas the batteries were charged up. |
Yorkshire
|
In service. |
Fowler
|
In service, no change from last time. |
Hunslet
|
No change from last time. |
South Devon Diesels' Drewry 04
|
Has been waiting parts or a replacement for the exhauster.
A replacement has now been obtained from a class 08. |
Stock
|
MINK - W 104700 - No change
CCT - W94556 - No change.
SHOCK - No change
MINK `B' W125814 - Two of the new doors were hung on
Thursday 12th October. The following Sunday the opposite side doors were
fitted and the van was moved outside.
BG - - Purcahser found for this van, so a start on cutting
it up was made also on Thursday 12th October and by mid November it had
become a flat wagon. A buyer for the frames & bogies may now have been
found! |
Other
|
Keep the aluminium drink cans coming in. |
Dates for Diary (Diesels running)
|
We understand that May 18th and 19th 2002 will be a diesel
working weekend; more later.
Slide Show: The Great Western Hotel (Opposite Exeter
St. Davids Station), Friday 08th February at 20.00hrs |
Working Weekends
|
Mostly Sundays at the moment.
If you turn up about between 09.30 and 10.00 someone
will be around. But no guarantees on this. |
Running Days
|
No running days left in 2001, have to wait until
2002 (see diary above). |